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3-10-08 It has been a very busy Month! Turn out over the last Month has not been very good with a significant amount of effort being spent on repairs to the operational engines with only restoration of the Fairmaid making any real progress. Work on the Sentinals has been halted for the time being and progress on the Austerities has all but ground to a halt due to a lack of available volunteer resource however the pistons are both now in No.19, wasted cylinder cover studs have been replaced, completion of the lubrication systems on No.7 and painting of the cabs, bunkers and wheel sets for both is in progress. A new pattern has been made for the blastpipe. Standard Tank 80105 is back from its visit to Wensleydale. The engine has developed quite a bad leak from the water space under the bunker. It is hoped that access can be made from the void beside the bunker to weld in a new repair plate. There is also attention required to the boiler with a leak from a foundation ring rivet or patch screw and there are a very large No. of stay nuts needing replacement etc. The engine has had many failures of main axle springs of the last couple of seasons and is an issue that is to be investigated. No. 1:- The boiler has been tested after all the tubes had been expanded, the RH bigend refitted, and returned to service. The engine failed a couple of weeks ago with a badly leaking boiler tube which is in the process of being replaced. The blastpipe has been found to be badly cracked at its mounting flange. The locating studs were very badly corroded and are in the process of being drilled out and replaced. It is hoped that the blast pipe can be repaired by welding. LNER D49 'Morayshire' has had a successful visit to Embassy and Bolton Abby Railway and is now back at Bo'ness and in Service. CR 419:- The engine is in service. See photos of recent activity by Alex livingstone and Tony Dance.

New bearing Fairmaid

New bearings Fairmaid

Fitting RH Big end bearing No.1

Suspect patch srew/rivet 80105

Removing grate 80105

At Bo'ness during film charter

Leaving Bo'ness during film charter

Neilly adjusting packing 'Morayshire'

419 being used to shunt 37409

37409 ready to depart

Fairmaid with cab refitted

Morayshire's tender ready to go to Bolton Abbey

Morayshire ready to go to Bolton Abby

Jim inside fire box 80105

Norman opening inspection door in water space 80105

Tom cutting out leaking tube No.1

Damaged studs replaced on cylinder covers No.19

Cleaning debris form rebore of cylinders No.7

Preparing cladding for paint Fairmaid

Pistons fitted to No.19

New Austerity blastpipe pattern

New Austerity blastpipe pattern

New Austerity blastpipe pattern

New Austerity blastpipe pattern

New Austerity blastpipe pattern

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Captions please!

New Austerity blastpipe pattern

Neally captures the leading lady!

1-09-08 Standard tank 80105:- The engine is operational at the Wensleydale Railway. 2 axle springs have broken and have been changed. Morayshire has had its boiler washout and is having various leaks fixed. Before the engine goes off to the Embsay & Bolton Abbey Steam Railway   419:- is in service. No. 1:- All the firebox tube plate leaks have been fixed and the RH big end bearing is ready to fit. Fair Maid:- Work is well under way to repair the water tanks and bunkers. No.7:- the machining of new side rod bearings continues. No. 19 The side rod bearings have been pressed out prior to white metaling and machining. See photos of recent activity by Alex Livingstone.

No. 19 side rod bearings press out

No.1 RH bigend ready to refit

Fair maid bunker/tank repairs

Fair maid bunker/tank repairs

Fair maid bunker/tank repairs

 

24-08-08  Standard tank 80105:- The engine returned from Aviemore worked the service trains of our Thomas weekend and went off to the Wensleydale Railway where it will be in service until the 7-09-08. Morayshire:- The engine is in service and is currently in daily use on the service trains. 419:- The engine is available for service. No.1:- Almost all the tubes at the firebox end have been expanded to resolve leaking between the tubes and the tube plate. The right hand big end bearing has been removed and re-machined. Fair maid:- The new axles have been returned complete with new tyres and the new crank pins fitted. All the side rod, connecting rod and motion pins and bearings have been replaced or re-machined. The cab roof has been repaired and fabrication of the new water tanks is in progress. No.19:- The Left Hand piston has been lapped to it's piston rod and is ready to be fitted.  See photos of recent activity by Alex Livingstone.

Alex machining the LH Big end bearings faces.

LH Big end bearing rebored.

No.1 RH bigend bearing machined ready to refit

Fair Maids Wheel sets ready to fit.

 

29-07-08 Turn out over the last couple of weekends and Monday evenings has been quite low due to holidays, however progress is being made! Fair Maid:- New slide bars have been made and the engine is now ready for its wheel sets. Delivery of the completed wheel sets has been delayed for a few weeks. No.19:- The RH piston has now been fitted and the front buffer beam is painted and ready to be refitted. 80105:- The engine is in service at the Strathspey Railway. 2 new axle springs have been fitted to the drivers. The engine is due back to Bo'ness next week. No.1:- The very badly worn LH big end bearing has been re-machined and refitted. The top 3 rows of tubes have been expanded and more may have to be expanded if the work carried out so far has not cured all the leaks. This engine will be in service for the next 'Thomas' event which starts on the 8th August. 419:- Is in service with no issues. Morayshire:- The engine is in service with no issues. See photos of recent activity by Alex Livingstone

Jim setting up big end bearing for boring No.1

Jim and Tom refitting LH big end No.1

Jim and Tom refitting LH big end No.1

The web master in best white suit before getting in the fire box to expand tubes

Expanding tubes No.1

New side rod bearings turned ready for drilling No.7

New Piston fitted to No.19

Regulating valve Westinghouse pump

Regulating valve Westinghouse pump

Machining in progress of new cover

Dick machining new end cover for Westinghouse Pump

After expanding tubes!

16-07-08 A great turnout on Monday 7th but very quiet on the 14th. Recently the turnout over the weekends has been excellent. Fair Maid:- The cross heads have been refurbished and the re-tyred wheel sets complete with new axles and pins are due back next week. No.7:- progress continues with the lubrication pipework and new cab doors have been made and painted. The valve spindle packing assembly has been removed and cleaned. No.19:- The right hand piston has been lapped to the piston rod and rings fitted ready for assembly. No.1:- The engine has been withdrawn from service due to leaks from the firebox tube plate. The tubes are to be expanded to resolve the issue. 419:- A tube started to fail early last week and the engine was failed and withdrawn from service last Thursday. On Saturday the offending tube was removed and a new tube fitted. The engine was returned to traffic but again failed on Sunday with a broken steam valve spindle. A new spindle was made on Monday evening, refitted and the engine returned to traffic on Tuesday. Jim's recent work on refurbishing the control valves for the westinghouse pump have been very successful with the pump performing very well. Morayshire:- The engine is due to have a boiler washout this coming weekend. Ranald:- reassembly of all the boiler and cab fittings is underway. See photos of recent activity by Alex Livingstone

Boiler refitted to Ranald

Front buffer beam being cleaned ready for painting No19

Billy working on lubrication pipework No.7

Delivery to site of refurbished merry go round hopper wagon

Detail of new lubrication pipework No.7

Dave preparing buffer beam for painting after damage repaired by welding No.19

Gerry needle gunning wheels No.19

Dave priming front buffer beam No.19

Young Craig Gordon helping to lap piston to rod No.19

Young Craig Gordon helping to lap piston to rod No.19

Lowering piston rod into place No.19

Lowering piston rod into place No.19

Piston rod read to be refitted No.19

419 heading for Birkhill 15-07-08

New tube plate tapping machine

419 steam valve components with broken stem and new material

Simon Sparkes operating the shaper

Cleaned valve spindle seal No.7

Refurbished crossheads and rear cylinder covers for Fairmaid

Yours truly with new spindle

New steam valve spindle being checked for fit. 419

The restored DMU on its way to Manual

DMU at Bo'ness

DMU at Bo'ness

 

5-07-08   Apologies for the late updates! I intend to update the site about twice a month from now on. The boiler has been lifted back into Sentinal Ranald. Work continues on the Fair Maid with the motion now all rebuilt. The work on the Austerities continues:- No.7 machining of new side rod bushes, new Vacuum brake pipe work, new graduated steam brake valve pipe work and lubrication pipe work is progressing well. The front draw hook is bent and the spring has seen better days! A potential replacement hook has been located. The hole in the buffer beam for the draw hook is also badly worn and will require attention before reassembly. The buffer beams for both engines have been needle gunned and primed ready for reassembly. No.19:-  new graduated steam brake valve pipe work is progressing well and the wheel sets have been needle gunned and primed.  See Photos of recent activity by Alex Naithsmith

Broken draw hook spring No.7

Peter machining

Fair Maid Motion

Fair Maid Motion

Gerry removing scale No.19 wheel sets

Gerry Removing scale No.19 wheel sets

John working on Fairmaids motion parts

John Glennon

Peter McDonald

New pipework in progress No.7

No. 19 front draw hook spring in good condition!

No19 pipework

 

11-06-08 BR Standard tank 80105 is now operating at Strathspey Railway for the next couple of Months. LNER No.246 'Morayshire' is in service at Bo'ness. Recent repairs have included welding up pin holes in 3 of the superheater elements and bushing and removing excessive wear on the regulator valve linkage (at the valve) The exhaust steam injector has been dismantled cleaned and leaking joint replaced. Costs for the supply, fit and turning of the new tyres for the driving wheels are being sought as well as a new set of superheater elements. No.1 is available for service as is 419 although Jim Verth is doing some tinkering with the Westinghouse pump! Good progress is being made on the Austerities with the cylinder valves faces being machined and the new pistons and rings being ready to fit to No.7. The mechanical lubrication pipework is also progressing well. New vacuum brake pipework has also been made up but will not be able to be completed until the front buffer beam has been refitted. The replacement cab doors for No. 7 are being made. The cross head slippers for both Austerities are being re-metalled and machined. Fair maid:- All the valve gear and motion has now been refurbished and is ready to be reassembled.

See photos of recent activity by Alex Livingstone

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25-05-08 The Thomas event went off very well with 80105, 419 and No.1 in service. The regulator mechanism on Morayshire has been refurbished by bushing and making new pins for the linkage to the regulator valve. The primary focus of restoration effort is now being directed to the Austerities. The imminent tasks to be carried out include refitting the pistons, piston rods and valves to the cylinder block and refitting the front buffer beams, machining new and refurbishing side rod bearings, re-metaling the cross head slippers, reassembly of the valve motion and re-wheeling. These are just some of the main tasks to be undertaken but there are hundreds of smaller tasks to be carried out as well before we tackle the boilers! We really need your assistance and if you can assist please come down on a Saturday/Sunday or Monday evening. You will be made most welcome!

See photos of recent events.

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18-05-08 No.1 has had its new tanks fitted, steam tested and repainted just in time for our Thomas event. Most effort over the last few weeks has been directed to putting No.1 back together and preparing for its steam test. 419 is in service. 80105 is going off to the Strathspey Railway for June-July and is currently in service at Bo'ness. Some work has progressed on the Austerities with  progress on No.7s lubrication system, new vacuum pipe work and manufacture of new side rod bushes etc. Progress is being made with the new boiler cladding for the sentinals. See photos of recent activity by Alex Livingstone.

Double-click to add photos

 

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